ABOUT ME and THE BITCH (Christine) and OUR UP'S and DOWNS - HOPE IT MAY SAVE YOU SOME OF THE PAIN and THE TEARS, THROUGH THE GOOD TIMES and THE BAD - MAINLY BAD....... BUT HEY, WHEN ITS GOOD - ITS BEEN FUCKING GREAT!
Tuesday, 29 September 2015
Tuesday, 22 September 2015
Thursday, 17 September 2015
once the rain had stopped on saturday, a trip to SoLow choppers
cute little hot rod yam with special crank built by fenland chops, here for some motor fettling
oh dear, Clives son Jay has had a few probs, they found a blown head gasket caused by damaged oil drain in the head
Clives new ride with ten overs
super cafe ally
as usual made welcome at the shop, the back roads were clear on the way back, no more god knows what over my face!
Wednesday, 9 September 2015
TripOut 4 and some of the coldest nights but spent with the warmest people
Stockers, featuring Leighton, Toddy & West
My good Friend Stan
kept us all amused and medicated
Baz and Johno
The lovely Sue and Captain Spike
Some of our happy campers
Nick at work
Toddy with his new customer build
devil in the detail
in situ
Toddys new personal build
has stocker detail
hand lettered
Baz's Knuckle
Toddys Stocker paint Job
Stockers
She ran strong and started on one kick after the show
Thursday, 3 September 2015
When something small can cause a bigger problem...
So after replacing the kicker gear I checked my timing and the light stayed on
These New 1000 mile Blue Streak Points
have somehow detached there bottom contact so are open all the time
and caused the advanced timing that caused the kickback that caused the kicker cog to break and crack the kicker cover.
Hope the Crank Pulley Holds as we are off to the TRIP OUT tomorrow
Tuesday, 1 September 2015
August Tale End Tales
up on the lift again seems constant every week now
to find source of noise - refit a new kicker gear and find out why the timing is advanced and nearly had my leg off.
The crank seal leaks still its not from the little screws holding the regulator wires
I took it off put on a smaller o'ring 9 although its not leaking down the grooved teeth of the crank and this time pushed it on flush up to the bearing. Somehow I don't think that will work.
I found the pulley was loose causing the noise - but the nut wasn't!
My fault. The washer I used previously which was thicker than the one originally supplied was not going over the shoulder on the crank. (the inner diameter is 7-10 thou smaller). Somehow I didn't notice and that little o'ring I put behind the crank seal was too big. and pushed everything forward. I was going to replace it but the spare replacement seal didn't arrive till Saturday and I had already got other problems to deal with!
So I now have to get a new pulley - £100 - OUCH
And finally -
I fitted a a new IRIS Xring chain two weeks ago - the previous one lasted 13000 miles! I should have taken it off at earlier at 10000 (heh heh) as thats when it started to need adjusting after every outing although not loose on sprocket.
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